So, in order to reset my new VP for F1M, I had a spring winding session 
yesterday. The original spring was something like 7 turns of 0.3mm 
(0.012") around a 1.5mm (0.06") mandrel, but this seemed to be too soft. 
The pitch only started to reduce halfway into the flight, and then went 
to bottom setting rapidly.
Looking at Bill's notes, I changed to 0.4mm (0.016") wire and 3 turns 
around the same mandrel. However, this seemed way too stiff, with 
practically no pre-tension I got the change to happen at reasonable 
torque, but then the VP did not go to bottom stop at all but was left 
hovering inbetween the stops. No good, too hard a spring. So eventually 
I went back to the thinner wire and a thinner (1.2mm, 0.047") mandrel. 
At 3 turns and 90 degrees pre-tension this seemed to work better. 
Tomorrows trimming session will show if this spring is any harder than 
the old one.
A question, however. I seemed to have hard times bending the spring so 
that it did not flip sideways. The old one with more turns took better 
support from the shaft tube, but the new was so flat that it did not 
support, and often it turned to the side. I tried bending the bottom 
with a slot that goes around the cross bar so that it would support 
there from flipping, but it was not too successful. Making a deeper hole 
in the adjustment screw gave better support. But is there something in 
the spring geometry that I have not realized, something that would make 
it inherently stable instead of unstable, locations of the support point 
for instance?
-Tapio-
Received on Thu Sep 06 2012 - 21:39:08 CEST
This archive was generated by Yannick on Sat Dec 14 2019 - 19:13:47 CET